The Waste Treatment and Immobilization Plant (WTP) currently under construction for treatment of High-Level Waste (HLW) at the Hanford Site will rely on cross-flow ultrafiltration to provide solids-liquid separation as a core part of the treatment process. To optimize process throughput, periodic chemical cleaning of the porous stainless steel filter elements has been incorporated into the design of the plant. It is currently specified that chemical cleaning with nitric acid will occur after significant irreversible membrane fouling is observed. Irreversible fouling is defined as fouling that cannot be removed by backpulsing the filter. PNNL has investigated chemical cleaning processes as part of integrated tests with HLW simulants and with actual Hanford tank wastes. To quantify the effectiveness of chemical cleaning, the residual membrane resistance after cleaning was compared against the initial membrane resistance for each test in a series of long-term fouling tests. The impact of the small amount of residual resistance in these tests could not be separated from other parameters and the historical benchmark of >1 GPM/ft2 for clean water flux was determined to be an adequate metric for chemical cleaning. Using the results from these tests, a process optimization strategy is presented suggesting that for the simulant material under test, the value of chemical cleaning may be suspect. The period of enhanced filtration may not be enough to offset the down time required for chemical cleaning, without respect to the other associated costs.
Revised: June 11, 2012 |
Published: May 10, 2011
Citation
Billing J.M., R.C. Daniel, R.T. Hallen, P.P. Schonewill, R.W. Shimskey, and R.A. Peterson. 2011.Chemical cleaning of porous stainless steel cross-flow filter elements for nuclear waste applications. In American Filtration and Separations Society Annual Meeting, May 10-12, 2011, Lousiville, Kentucky. Kingwood, Texas:American Filtration & Separations Society.PNNL-SA-79432.